青草沙水库排水闸加大泄量后的消能防冲研究-学兔兔 www.xuetutu.com
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2019-03-05 23:08:00
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青草沙水库排水闸加大泄量后的消能防冲研究-学兔兔 www.xuetutu.com水利水电技术第44卷2013年第12期青草沙水库排水闸加大泄量后的消能防冲研究丁星星,谢东(1.河海大学水利水电学院,江苏南京210098;2.上海友为工程设计有限公司,上海200333)摘要:青草沙排水闸增大泄量到300m/s时下游将发生远驱水跃,现有消力池需要采取相应的加固措施。经水力计算和水槽试验,建议采用海漫段定点抛投四面体的海漫加糙方式,四面体棱长l111,呈梅花状布置,顺水流和垂直水流方向,中心点间距与棱长之比2:l,共布置5排,其壅水效果与稳定性均可满足要求。关键词:青草沙排水闸;消能防冲;海漫加糙中图分类号:TV653(255)文献标识码:A文章编号:1000—0860(20l3)12.0051—04ResearchonenergydissipationanderosioncontrolofQingcaoshaSluiceafterdischargeincreaseDINGXingxing,XIEDong(1.CollegeofWaterConservancyandHydropowerEngineering,HohaiUniversity,Nanjing210098,China;2.ShanghaiYouweiEngineeringDesignCo.,Ltd.,Shanghai200333,China)Abstract:TherepeⅡeddownstreamhydraulicjumpwilloccur,ifthedischargereleasedfromQinsc~haSluiceincreasesto300m3/s,andthenthecorrespondingreinforcementmeasuresmustbeadoptedfortheexistingstillingbasin.Throughthehydrauliccalcula—tionandlaboratoryflumeexperimentconcerned,itissuggestedtoplaceconcretetetrahedmnsatthefixed-pointsforrougheningtheapronsectiontherein.Theedge—lengthoftheconcretetetrahed
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